Palmdale Fuel Cell Project Review 090727
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Transcript Palmdale Fuel Cell Project Review 090727
The Palmdale Fuel Cell Project:
Five-Year Review
SCAP Energy Management Committee
Meeting
Mark McDannel
Los Angeles County Sanitation Districts
July 28, 2009
Presentation Overview
Facility Descriptions and Design
Parameters
Results
Lessons Learned & Conclusions
Antelope Valley Green
Energy Program
Parallel renewable combined heat and
power projects using digester gas
Similar size units at similar size plants
250 kW Fuel Cell Energy molten
carbonate fuel cell at Palmdale
250 kW Ingersoll-Rand microturbine at
Lancaster
Palmdale Water Reclamation Plant
STARTED: NOVEMBER 1952
CAPACITY: 15 MGD
CURRENT FLOW: 9.2 MGD
Project Design Data
Manufacturer
Fuel Cell Energy
Rated unit output, gross
250 kW
Net system power output
225 kW
Startup date
2005
Electrical efficiency (LHV)
47%
% of heat input recovered as waste heat
26%
Combined heat and power efficiency
73%
2005 Performance Test Data
Gross power output
251 kW
Electrical Efficiency
46%
Palmdale Fuel Cell Project
Fuel Cell Energy molten
carbonate fuel cell
Capital cost $2.4
million
50% of cost recovered
from SGIP
Fuel Cell Project Team
Quinn Power Systems Associates
Prime contractor
Operation and maintenance under contract to LACSD
Fuel Cell EnergyFuel cell supplier
Subcontracted to Quinn for fuel cell O&M
SCS EnergyDesign and installation
Gas treatment skid o&m
Facility ownership retained by LACSD
Fuel Cell Fuel Skid
Load Profiles at Palmdale
Electricity Purchase Load Profile With and Without Fuel Cell In
Service (typical days)
400
350
Fuel cell at full load
Fuel cell out of service
250
200
150
100
50
0
0:
00
0:
45
1:
30
2:
15
3:
00
3:
45
4:
30
5:
15
6:
00
6:
45
7:
30
8:
15
9:
00
9:
45
10
:3
0
11
:1
5
12
:0
0
12
:4
5
13
:3
0
14
:1
5
15
:0
0
15
:4
5
16
:3
0
17
:1
5
18
:0
0
18
:4
5
19
:3
0
20
:1
5
21
:0
0
21
:4
5
22
:3
0
23
:1
5
Load (KW)
300
Time
Results
Plant Performance
Economics
Siloxane Removal
Lessons Learned & Conclusions
Fuel Cell Availability and
Capacity
Availability
Capacity Factor
90%
76.5%
80%
70.2%
69.8%
70%
60%
50%
58.2%
42.6%
41.5%
35.8%
40%
31.8%
30%
20%
10%
0%
2005
2006
2007
2008
Fuel Cell Availability and
Capacity
Availability has increased during the
program
Capacity has decreased despite
improvements in availability
Capacity factor well below 90% target
Breakdown of Downtime
70%
Unknown/Other
Planned Outage
Districts' Equipment
SCE Grid
Fuel Skid Outage
Power Equip. Outage
% Time Unavailable
60%
50%
40%
30%
20%
10%
0%
2005
2006
2007
2008
Palmdale Availability
Fuel cell balance of plant equipment
Routine repairs on water treatment system
Multiple significant fuel skid issues
Four electrode stack replacements
Carbon filter media replacement
Stack Replacements
Four stack replacements
3975 hrs - Replaced with new stack design
2696 hrs – Stack degradation
5386 hrs - Sulfur poisoning & excessive
startups
9889 hrs - Sulfur poisoning
Causes of Capacity Reduction
at Palmdale Fuel Cell
Frequent long time periods at reduced
loads due to fuel cell issues
Variations in digester gas pressure due to
issues with the fuel skid
Lower digester gas flows and higher
methane content due to sewer cleaning
Defective stack installed in 2008
Causes of Capacity Reduction
at Palmdale Fuel Cell, ctd
Long start up times after outages
Parasitic Loads
Internal fuel cell loads of 18-20 kW not counted
against net, but cost plant when fuel cell is in hot
standby
Fuel skid, 25 kW (design value, not metered)
Three sulfur poisoning events have resulted in
reduced power output for several months
Q1 2009
Q4 2008
Q3 2008
Q2 2008
Q1 2008
200
Q4 2007
Q3 2007
Q2 2007
Q1 2007
Q4 2006
Q3 2006
Q2 2006
Q1 2006
Q4 2005
Q3 2005
Q2 2005
Q1 2005
Net Power, kW
Net Electrical Generation per
Quarter
260
240
220
Rated Net Output
180
160
140
120
100
80
60
40
20
0
Other Issues at Palmdale
Integration into plant digester gas system
including flare and boilers was complex
Remote monitoring and operation help
minimize down time
Installation of natural gas line was
necessary for backup and controlled
shutdown
Capital Cost
Fuel Cell
$1,178,000
Fuel Treatment Skid
$201,600
Installation
$526,301
Control Room Signal
$2,895
Gas Piping Installation
$2,511
Satellite Internet
$5,328
Warranty
$330,000
Sales Tax
$113,817
SCE Interconnection
$3,038
Natural Gas Piping
$19,084
Total Capital Cost
$2,382,574
SGIP Rebate
-$1,125,000
Net Cost to Districts
$1,257,574
Facility Economics (design,
assuming 90% capacity factor)
Capital Cost
$2,382,574
Subsidies
$1,125,000
Net cost
$1,257,574
Annual power purchase savings (at 90%
capacity factor)
$227,000
Total subsidized production cost /kW-hr
$0.093
Operation and maintenance /kW-hr
$0.035
Capital recovery /kW-hr
$0.058
Retail electricity cost /kW-hr
$0.128
Cost of Power Production
$0.35
$0.28
$0.30
$0.041
$/kWh
$0.25
$0.049
$0.20
Natural Gas
O&M
Average Retail Electrical Price
$0.15
Capital Recovery
$0.093
$0.10
$0.190
$0.035
$0.05
$0.058
$0.00
Design 90% C.F.
Actual
Net Savings per Year
2005
2006
2007
2008
$66,551
$69,452
$46,543
$2,119
Cumulative Net Savings
$1,400,000
$1,200,000
$1,257,574
Capital Cost to Districts with
SGIP Grant
$1,000,000
$800,000
$600,000
$184,665
$400,000
Net Savings Earned through Dec 2008
$200,000
$Dec- Mar04
05
Jul05
Oct- Jan- May- Aug- Nov- Feb- Jun- Sep- Dec- Apr05
06
06
06
06
07
07
07
07
08
Jul08
Oct- Jan08
09
Siloxane Removal
Carbon absorption
Also removes Cl, S to protect fuel cell
Requires periodic testing for
breakthrough
Short term high siloxane levels could
cause undetected breakthrough
Criteria Pollutant
Emissions
NOX
0.05 ppm @ 15% O2
0.0017 lb/MWh
CO
1.2 ppm @ 15% O2
0.025 lb/MWh
TGNMO
2.07 ppm
0.016 lb/MWh
Sulfur Compounds
Raw
Digester Gas
Treated
Digester Gas
H2S, ppm
20
ND<0.5*
Total Reduced Sulfur, ppm
20
ND<3.5
*Note-detection limit not sensitive enough to fully
protect fuel cell
Trace Organic Compounds
Raw
Treated
Digester Gas Digester Gas
Exhaust
Chlorobenzene, ppb
38
2.1
ND<0.05
Vinyl Chloride, ppb
2.0
0.38
ND<0.05
Benzene, ppb
26
2.4
0.95
Toluene, ppb
830
36
ND<0.27
Recent Operating Status
Stack replaced in Sep 2008.
A leak in the new stack forced reduction
in output to 40 kW in Dec 2008
Operated at nearly 100% availability at
reduced load
Fuel cell was shutdown June 11 upon
discovery of sulfur breakthrough
Unit will not be restarted
Lessons Learned by
LACSD
Ambient temperature considerations
Chiller was undersized for high summer temperatures
Lower digester gas production during winter months
Carbon media must be monitored and/or
replaced periodically
Site involvement
Digester gas system balancing
Lessons Learned by Fuel
Cell Energy
Natural gas must be used as a backup
fuel
A load bank should be installed to
mitigate grid disturbances
Ensure proper maintenance of the fuel
skid
Contracting Issues
Impacting the Facility
These were demonstration projects; as such, providers
would not provide availability guarantees
The current O&M contracts have no performance
incentive or penalty: down time costs the owner but
does not cost the contractor
Fast response not always justified by plant economics
Other contracting options
Incentives and penalties for response time and availability
Power purchase agreement, unit owned by provider or third
party
These options are generally currently available
Conclusions
The Palmdale fuel cell did not meet
performance goals
The Palmdale fuel cell met its goal to
demonstrate a high efficiency, low
emission technology on digester gas
As an early adopter, Districts allowed
manufacturers to address and resolve
design and operating issues
Questions?
Contact information
[email protected]
(562) 908-4228 x2442